Soo....I've finally gotten a chance to actually revise and edit my paper for my senior design project....only 4 months after I handed it in. I got an A anyways, and I only found one or two blaring mistakes ;). But, there are just way too many amazing pictures that tell the story of making this thing beyond simply a report on the design, procedure, and results. So, I'm going to move ahead and get some of these great pictures of "real engineering" (as stated by Prof Maxworthy during our presentation).
I just thought that I'd post the end result first...

So this piece down here was essentially the basis of my project. This is the aft bulkhead and the most difficult part of the project to machine and get just right. The internal structure of this has two steps in it, one for the nozzle to rest in and another for the fuel to rest in. I had never machined anything like this before, so it was an experience and definitely a time to get it right (each disc of alumnium cost $30.00). I managed to get the two sets machined to within 5 thousandths of an inch in diameter and depth, within the tolerances that I needed. More importantly, the nozzle and the grain fit in perfectly. Seen below is a tapped 1/4-20 NPT hole for a NPT to AN fitting for the injection into the nozzle. The holes around the collar are for mounting the motor to the thrust stand.





So...the plan was that I would start the pressure off at something like 20 or 30 psi, and then increase the pressure on the regulator until I choke the flow. Well, I saw the smoke and opened up the ball valve and the motor just went, and it screamed. All I can think of as I'm watching this thing is "please don't blow up, please don't blow up" and I'm seeing this big bubble near the injector get bigger and bigger. That 7 seconds of burning felt more like 20 and I just turned it all off because I didn't know what to expect at all. Great learning experience and I was stoked after this fired. I actually made a rocket motor, from scratch, it ran for a whole 7 seconds., and I still had all 10 fingers. Just watch the video below and you can hear my excitement.
After those seven seconds of sheer terror, we got everything disconnected to check out the damage. Amazingly, everything looked great. We realized that the throat for the nozzle was too large to support the flow rate that we could supply, or that may have simply been the pressure that we were running at. There was an odd place in the fuel where near the injector that burned much faster than at other points in the injector, and we deposited a good layer of carbon on the injector face. Other than that, the motor performed amazingly well and worked.



This is how the motor was integrated into all of this. In all honesty it was really simple from a plumbing and design standpoint.

And here are the three videos that gave my group and me A's.
Those three test fires were all from that Tuesday night before the project was due. There was about an hour recycle time to get everything disassembled, cleaned, check out the video, get everything prepped for firing again and firing. The biggest pain in the ass was the igniter. For what ever reason we would get it put together, test the continuity and everything would check out. We'd get it in the motor and have everything ready to go, short out the igniter and it wouldn't work. We took it all apart again, put it back together and got it back in the motor and voila, it'd work. Never worked the first time but always worked the second time. So, we got our motor burning with a head end pressure of 100 psi, hopefully a motor pressure of ~50 psi, and let it burn as long as we felt comfortable. Originally this was going to be 18 seconds. The first test fire was 7 seconds. Those three motor tests ran for about 30 seconds plus/minus 2 seconds. Having being the one operating the oxygen....those thirty seconds were actually about 3 minutes, maybe 10 in my mind. I don't know if you can hear me screaming in those videos asking for a time count, but the motor was so loud you couldn't hear anything. I was amazed at the scream a little 1/8" diameter hole could make, and it was awesome. I was more surprised that we didn't get the attention of the campus cops for making that much noise at 11 PM, 12 AM and 1 AM, cause it was loud.
So, all of our data was taken (those three videos) and managed to say from those (the last video around 28 seconds after ignition) that we manipulated the flame, but didn't necessarily produced a sustained thrust vector and definitely didn't have complete control authority over that thrust vectoring. All in all my group managed to write the papers from Thursday night at 6 PM to Friday morning at 6 AM, got those sent off to Kinkos to be printed and bound, burned a CD with the videos and handed it all in. I think I slept 15 or 16 hours that week, but got everything finished. It was one of the coolest projects that I've worked on so far, but I'd like to make this my baseline for my future projects.
So, all of our data was taken (those three videos) and managed to say from those (the last video around 28 seconds after ignition) that we manipulated the flame, but didn't necessarily produced a sustained thrust vector and definitely didn't have complete control authority over that thrust vectoring. All in all my group managed to write the papers from Thursday night at 6 PM to Friday morning at 6 AM, got those sent off to Kinkos to be printed and bound, burned a CD with the videos and handed it all in. I think I slept 15 or 16 hours that week, but got everything finished. It was one of the coolest projects that I've worked on so far, but I'd like to make this my baseline for my future projects.
1 comment:
Nice work, Chris. Saw the link from your Facebook - awesome pictures, too!
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